
Photo courtesy of Bill Gee
- Mar-16-2002
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The original Tuber was one of my standard
fliers; I flew it nearly every time out.
Inspired
by the Rocket Vision Six Pack, the upper stage of the Tuber
used six tube sections (BT-55) as its fins. To complement the six
tubes, the booster was equipped with 6 balsa fins. It came out
looking quite good. And the Squirrel Works were impressed enough
to kit the Tuber.
In the original, both stages used 18mm motors. It flew great on
B's and C's, and
with its high drag, the Tuber was great on small fields using a B6-0 to
B4-4 combination.
And the tube fins proved quite rugged.
The original Tuber had a history of accidents. At least
three times it came in on plastic wad recovery, or worse, stuck
chute. In some cases, it seemed the parachute just stepped aside
and allowed the ejection gasses to escape without
ejecting the chute. But each
time it was able to fly again without repair.
Over time, Tuber's nose cone got dinged up some, and there were plently
of cracks in the paint, but it proved to be quite rugged, and
always entertained
me. However, it met its demise just before
Christmas of 2002 when it core sampled in a concrete parking lot.
It was almost totally destroyed, but the nosecone was salvaged,
and used on its successor.
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The replacement featured 24mm motor mounts
and an extra booster stage. The repaired nosecone had a slightly
rounded tip, but otherwise, the rocket's shape was true to the
original. A nice decal adorned the new Tuber.
Soon after entering service, on a 2-stage flight, the upper failed to
light, and the resulting lawndart accordioned the airframe and
destroyed the nosecone 
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So the new Tuber was repaired. I
turned a replacement nosecone out of cedar, and spliced in a new
section of
airframe. Some dings on the second stage booster were repaired
and painted blue. Rebuilding the rocket, I was a little too
creative and failed to be true to the original. The nosecone was
too long and the wrong shape. And the repaired airframe was too long as
well.
At left, the rocket is ready for its only flight in this
configuration. The motor stack was D12-0 to D12-0 to D12-7.
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Here's a liftoff shot of the D-D-D combo. The rocket was too
heavy for the single D12-0 in the first stage, and
crawled off the rod. It soon began turning into the wind, and by
the
time the third stage motor lit, it seemed like it was going
horizontal. Don Magness
helped me track the flight, and we had a long walk but managed to
recover all the pieces.
The lengthened body tube and heavier nosecone proved to be unnecessary
and were in fact detrimental.
They contributed to weather cocking and gravity turning.
The lesson learned was that more thrust is needed to fly a stack like
this. |

Photo courtesy of Pelham
Swift
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Below is a great liftoff shot. The
rocket is in a rare configuration with
the airframe cut back to the original length, but still sporting the
cedar nosecone.
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Photo courtesy of Tim Sapp
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